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Date: 05 Apr 2007 18:12:57
From: Robert Harmon
Subject: Nuova Simonelli Mac Digit 1-group (long)
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I finished rebuilding the Mac Digit & before starting the rebuild of a Mac Personal, I thought this would be a good time to back off & encapsulate what I've done & the lessons I've learned. This is NOT a solicitation to sell this machine, but an effort to pass along some hard-learned knowledge to anyone contemplating such a project. First, let me acknowledge the good folks here in alt.coffee & Coffee Geek. The advice & help so generously provided was of enormous (indispensable?) help. I won't bother naming names - you know who you are & I want to just say that without you folks these groups would devolve into quickly oblivion. THANK YOU, ONE & ALL! I rebuilt the Mac for a friend who, when the job was finished, told me that his spouse didn't want the *thing* in her kitchen. He suggested a swap for an extra Mazzer grinder I had, so now I own this machine. In the rebuild process I started from a knowledge base of near-zero. I'd replaced rotary pumps, gaskets & a few other parts for friends with commercial machines. But this was to be my first *frame off* restoration of a professional espresso machine. Not easily daunted, I plunged recklessly into the project; as they used to say in the Army of the uniniated, "Fat, dumb, & happy". First I had to figure out how to get the exterior panels off. Neither the owner's manual or the parts manual gave up any clues, so I begged for help in alt.coffee & thankfully someone shared their knowledge. By removing four Allen bolts under the top cover & two long-headed (what else can you call them?) hex head bolts under the drip tray, the two side panels can be slid forward & off. The back panel required the removal of four bolts hidden behind the frame on either side of the boiler.The front panel removal required that the Inox panel surrounding the group be first removed. Loosen the two Phillips screws inside the panel that hold it to the front panel & remove the other screw that connects it to the underside of the control panel. Pulling open the ends of the panel frees it from the two loosened screws & it lifts out. Remove the four Phillips screws holding the front panel to the frame & lift it out. Once exposed the internals of the machine were open to inspection & easily accessed for repair. Here's where I used Paul Pratt's advice & started taking pictures of everything, from all angles. I then started removing the copper tubing & fittings. The boiler & group came out easily enough after a bit of head scratching & more than a few "Hail Mary's". At this time let me point out that before the acidic bath each part is soaked in a hot bath of industrial strength caustic detergent (otherwise the acid bath would be less effective). I have a heated tank used to degrease engine parts that agitates the solutions used around the parts. This is a tools not available to most enthusiasts, but if you strike up a good relation with *friendly* independent mechanics or parts store clerks you should be able to find one you can use. I pulled the element from the boiler & dropped it & the boiler into the tanks of hot solution. The boiler was in pretty good shape externally with the nickel plating intact & corrosion minimally present. Internal inspection revealed slight scaling & a discomforting(!) wear spot on the HX tube. I don't know if the element is coming into contact with the tube or if the wear spot is due to the close proximity of the HX to the heat source? I decided to alter the element's shape a bit to provide extra clearance just to be on the safe side. Once it's reassembled, I suppose the only way I'll know if there's a problem is when the HX ruptures & water starts flowing from the group when the pump is off? The group was soaked in the detergent bath only & all fittings were removed. While it was submerged, I ran a tube-brush, connected to a pneumatic wrench, through all of the passages. After this loving attention the group came out spiffed up (technical jargon) & like-new. For the copper tubing I jury-rigged a device that, at the risk of sounding less than humble, I like to think of as truly inspired. The copper tubing is connected using rubber surgical tubing to an Ulka pump. The pump's intake Nylon tube & the output from the copper tubing was submerged in a pot of acidic solution kept at 95 degree Fahrenheit. This recalculating warm solution was pumped through the tubing for up to an hour & cleaned the most badly scaled tubes to a gleaming like-new finish. (I was sorely tempted to trash the copper tubing & replace it with high-temp Nylon tubing. But, since this was not my machine at the time I opted to clean the copper instead.) When inspecting the machine prior to pulling it apart I saw a bit of rust & corrosion under the pump. After disassembly I found the "T" fitting for the outlet side of the pump was cracked. Other than it's replacement all other hard-parts (S/S, copper, brass) were reusable after cleaning. I did opt for new o-rings & gaskets & where I couldn't find the correct size or materials I opted for the ol' standby - Permatex RTV (NSF certified) sealant. This stuff is a must for anyone working with hi-temp water/steam systems - it & the other great standby, JB Weld, have saved me many times when a project was dead-ended because of an unobtainable of broken part. If you don't have these in your toolbox, RUN to the hardware store now 7 get some, because eventually everyone will need one or the other in a *hurry*. Thanks to the many pictures I took, reassembly went off relatively smoothly. Fittings were tightened, wires were connected, & the water & drain lines were connected. I turned the water on & filled the boiler after getting help figuring out that the pump has an auto shut off if it runs for too long. Powering the machine on & off until the boiler filled solved this issue. With just the mains pressure I let the machine sit powered on for 30 minutes to achieve a stable boiler temp. I checked for & found the expected small leaks. One o-ring was cut installing it (simple replacement fixed it), but everything else just needed to be tightened a bit to stop the leaks. I let it set the rest of the day without running the pump just to be safe, without finding more leaks. Yeah! I then began adjusting the pstat & pump pressures. I set the pstat to 1.2 Bar & the pump to a bit under 9 Bar (both based on empirical testing, using myself as the willing guinea pig). Using week old beans I eventually began pulling shots that were almost exclusively crema. Happy, Happy, Happpy! The exceptions to the easy reassembly were the plastic side & back panels. The mounting bolts screw into brass lugs that are pressed into holes formed in the plastic panel. Probably due to being dropped at some point, several of the lugs had been broken out of their holes (in fact this probably explains the cracked "T' fitting mentioned above). Aha, yet another job for JB Weld! After fixing this problem everything went together quickly. Boy, did this machine look good. If I didn't already have the Bunn ES-1A that I've grown to love dearly, I might have opted to use this machine for myself. That plus the plastic panels being a *very* boring charcoal grey made me decide to keep the Bunn & sell the Mac. There were many times I had to come back to the groups, sometimes for critical help & even more often for simple hand-holding reassurances. I could have successfully completed this project without this advice (the machine is way too simple to be *much* of a problem to figure out) but I would have made costly mistakes in doing it on my own, so once again I say THANK YOU to everyone that helped me in this project. -- Robert (Gig 'em!) Harmon www.tinyurl.com/34r5dx - My attempt at blogging. www.tinyurl.com/2tnv87 - Guidelines for coffee newbies. www.tinyurl.com/37gwfr - I have stuff available for sale.
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Date: 11 Apr 2007 00:36:21
From: diab0lus
Subject: Re: Nuova Simonelli Mac Digit 1-group (long)
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On Apr 10, 5:47 pm, "DavidMLewis" <DavidMLe...@mac.com > wrote: > On Apr 10, 12:45 pm, "diab0lus" <r0cketscient...@hotmail.com> wrote:> I looked for high temperature nylon tubing rated for >300F and >130 > > psi and wasn't able to find it anywhere. > > This is the tubing used throughout my Techno, and it's proved to be > quite reliable: <http://www.mcmaster.com/param/asp/PSearch2.asp? > reqTyp=parametric&act=psearch&FAM=tubing&FT_3498=156718&FT_104=141&session=tubing; > 3498=156718;104=141&sesnextrep=236747754368952&ScreenWidth=1280&McMMainWidth=868>. > If that doesn't come through, go to <http://www.mcmaster.com/> and > search for Teflon FEP. It's FDA approved and meets both the pressure > and temperature requirements handily. You'd still want to keep it well > away from a heating element, if for no other reason than damage in a > boil-dry scenario, but any other application inside the machine should > be fine. > > Best, > David Thanks for the link. I just finished all of the copper plumbing in Silvia tonight. I wish this conversation would have happened last week before my flow control knob arrived. Silvia is now tuned to 85 ml per 10 seconds water debit and has real pre-infusion (controlled by a switch on the front panel). I'll be posting about the preinfusion mod probably within the week. I'm not familiar with the Techno, so I don't know if this mod would be of any interest to you. Thanks, Ryan
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Date: 10 Apr 2007 14:47:23
From: DavidMLewis
Subject: Re: Nuova Simonelli Mac Digit 1-group (long)
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On Apr 10, 12:45 pm, "diab0lus" <r0cketscient...@hotmail.com > wrote: > I looked for high temperature nylon tubing rated for >300F and >130 > psi and wasn't able to find it anywhere. This is the tubing used throughout my Techno, and it's proved to be quite reliable: <http://www.mcmaster.com/param/asp/PSearch2.asp? reqTyp=parametric&act=psearch&FAM=tubing&FT_3498=156718&FT_104=141&session=tubing; 3498=156718;104=141&sesnextrep=236747754368952&ScreenWidth=1280&McMMainWidth=868 >. If that doesn't come through, go to <http://www.mcmaster.com/ > and search for Teflon FEP. It's FDA approved and meets both the pressure and temperature requirements handily. You'd still want to keep it well away from a heating element, if for no other reason than damage in a boil-dry scenario, but any other application inside the machine should be fine. Best, David
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Date: 10 Apr 2007 12:45:53
From: diab0lus
Subject: Re: Nuova Simonelli Mac Digit 1-group (long)
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On Apr 5, 2:12 pm, "Robert Harmon" <r_h_har...@Zhotmail.com > wrote: > badly scaled tubes to a gleaming like-new finish. (I was sorely tempted to > trash the copper tubing & replace it with high-temp Nylon tubing. But, since > this was not my machine at the time I opted to clean the copper instead.) I looked for high temperature nylon tubing rated for >300F and >130 psi and wasn't able to find it anywhere. I didn't think it existed. The only option I appeared to have aside from copper was PTFE (Teflon) tubing. I ended up using copper tubing in my project because I couldn't find PTFE in the length I needed and wasn't going to shell out $180 for 100 ft of it. Swagelok makes some very nice braided ss PTFE-lined hoses in various connections and lengths. They have one type that goes down to 1/8" tube size, so that gives you <1" bend radius. Ryan
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